DIY Check valve.
Posted: Fri Jul 28, 2017 3:34 pm
My compressor gave up the ghost.
No, not the big one with the DIY check valve, the anemic one. Trying to nail down floor sheeting, and for a while had to drive a nail, and wait a while. Drive another, and wait a while. Would have been faster to just break the nailgun nails apart and nail the floor by hand. LOL Then finally, it just gave up the ghost entirely.
Time to fix the BIG compressor...
Fix an oil leak. Fix a couple air leaks.
Replace a condenser. Now it starts up and runs beautifully!!
Until...
Well, it starts, runs, and fills up. Stops running, because it is at the upper pressure limit. Then, when the pressure reaches the lower limit, it tries to kick back on, but even the new condenser doesn't give it enough oomph to start back up.
Problem? Air pressure at the head.
There is a check valve at the end of the line that comes from the head to the tank. This valve screws into the tank itself. Then the copper line is attached to it. A check valve is essentially a one-way valve.
Just above the point where the air is not allowed to come back out of the tank, is the line that goes to the pressure switch.
The way it is supposed to work is...
The check valve prevents air from returning to the head. That line from the pressure switch also has a 'dump' on it. (Another way to know that your check valve is not working, is that you will hear air constantly escaping from that dump valve.) The check valve closes. The dump valve then dumps the residual pressure in the copper line. Now, when your compressor tries to start again, it is not fighting against all the pressure that is left in the tank. An "at pressure start" is the same as an empty tank start.
What happened is that my check valve actually broke. Physically. Looking at a new one, and comparing it to my old one, makes me wonder if their over engineered part is actually designed to fail... (Which is why I decided to fix it instead of replace it. My 'design' should last until after the compressor head has melted itself down from so much use...)
Here is a pic of a factory part:
When I took my check valve out of the tank, it was missing the entire bottom part. It was in essence just a straight-through pipe. Here is a pic of it straight through. (Sorry about the crummy pics from here on, I have the cheapest possible camera and it just doesn't want to focus.)
My first attempt at fixing it didn't go so well. I tried to simplify what they had done. Used a spring and a circle that I cut from a juice bottle cap. (Thick stuff. Has silicone rubber on one side. That side went toward the valve.) It just blew right off, just like the factory design itself had done.
Finally I gave up on trying to fix it the way they had done it in the first place, and go with what I knew would work.
Here are the parts to my new valve. The original valve. A 1/4-20 round head stainless screw. A spring. And a rubber faucet repair washer.
Down inside the valve body is a lip that the spring rests against. It probably would have worked fine, but I bent the bottom of the spring out just a bit, to be sure it stayed on that lip. The head of the screw was pretty much exactly the same as the OD of the spring. but to make sure that it never worked it's way past the spring, I bent the top of the spring to be an exact fit on the shaft of the screw. The pic of that is so bad that you can't even see what I am talking about, so no pic this time.
I can't add any more pics to this, Please delay responses until I have finished this. (I'll write finished at the end.)
No, not the big one with the DIY check valve, the anemic one. Trying to nail down floor sheeting, and for a while had to drive a nail, and wait a while. Drive another, and wait a while. Would have been faster to just break the nailgun nails apart and nail the floor by hand. LOL Then finally, it just gave up the ghost entirely.
Time to fix the BIG compressor...
Fix an oil leak. Fix a couple air leaks.
Replace a condenser. Now it starts up and runs beautifully!!
Until...
Well, it starts, runs, and fills up. Stops running, because it is at the upper pressure limit. Then, when the pressure reaches the lower limit, it tries to kick back on, but even the new condenser doesn't give it enough oomph to start back up.
Problem? Air pressure at the head.
There is a check valve at the end of the line that comes from the head to the tank. This valve screws into the tank itself. Then the copper line is attached to it. A check valve is essentially a one-way valve.
Just above the point where the air is not allowed to come back out of the tank, is the line that goes to the pressure switch.
The way it is supposed to work is...
The check valve prevents air from returning to the head. That line from the pressure switch also has a 'dump' on it. (Another way to know that your check valve is not working, is that you will hear air constantly escaping from that dump valve.) The check valve closes. The dump valve then dumps the residual pressure in the copper line. Now, when your compressor tries to start again, it is not fighting against all the pressure that is left in the tank. An "at pressure start" is the same as an empty tank start.
What happened is that my check valve actually broke. Physically. Looking at a new one, and comparing it to my old one, makes me wonder if their over engineered part is actually designed to fail... (Which is why I decided to fix it instead of replace it. My 'design' should last until after the compressor head has melted itself down from so much use...)
Here is a pic of a factory part:
When I took my check valve out of the tank, it was missing the entire bottom part. It was in essence just a straight-through pipe. Here is a pic of it straight through. (Sorry about the crummy pics from here on, I have the cheapest possible camera and it just doesn't want to focus.)
My first attempt at fixing it didn't go so well. I tried to simplify what they had done. Used a spring and a circle that I cut from a juice bottle cap. (Thick stuff. Has silicone rubber on one side. That side went toward the valve.) It just blew right off, just like the factory design itself had done.
Finally I gave up on trying to fix it the way they had done it in the first place, and go with what I knew would work.
Here are the parts to my new valve. The original valve. A 1/4-20 round head stainless screw. A spring. And a rubber faucet repair washer.
Down inside the valve body is a lip that the spring rests against. It probably would have worked fine, but I bent the bottom of the spring out just a bit, to be sure it stayed on that lip. The head of the screw was pretty much exactly the same as the OD of the spring. but to make sure that it never worked it's way past the spring, I bent the top of the spring to be an exact fit on the shaft of the screw. The pic of that is so bad that you can't even see what I am talking about, so no pic this time.
I can't add any more pics to this, Please delay responses until I have finished this. (I'll write finished at the end.)
Love these projects.